Well, that's Rheola done for the 2nd weekend and once again it was character building... in massive ways, both for me, him and in truth, most people
Fri started lovely, the weather was decent and we spent a couple of hours playing at Pontypool, just a bit of a warm up really, no reason other than "why not" and he was loving the bike.
Well, mostly... it had developed a creak.... which was then my job later on Friday to diagnose... That got interesting. I was stripping the bike down while he was out with Katy Curd on the track walk. I stripped pivots, linkages, everything, still got the noise.... WTF..
As i was putting the bike in the van, completely unweighted it creaked as i stopped... I ended up diagnosing it as a caliper bolt/caliper that was creaking.. Bit of a clean on the rear caliper/bolts and it was golden. The boy checked and confirmed. Awesome.
Sat brought... wet... rainy wet, again..
The bikes were coming back with their usual patina
IMG_20240413_130940 by
Steve Weeks, on Flickr
IMG_20240413_125559 by
Steve Weeks, on Flickr
But the boy was happy and seemed to be going well
The bike though, well that had developed a bit of play.. lol... yeah i know.. i know. We're talking minimal things here but i do like/try and have it 100% each start of the day so back at the AirBNB and i've stripped the back end down again and replaced the pivot bearings which i think got damaged in the Friday repairs... but it still wasn't 100%. So i thought it was the upper shock bearing, i removed shock and fitted a spare shock we have which is brand new. Perfect... Shock back out and top bushing replaced in the shock and off we went for Indian and a relax.
It's hard to put into terms how much it takes out of both riders and crew at times, it's full on for both sets, the rider because they're doing all the work and the crew for standing round for 7hours, the pressure, intensity, etc... it's just pretty tough. We were both in bed and asleep fairly handy. (Well he was asleep, i struggled with sleep for some reason, maybe because it was the first National? Dunno).
Sunday brought dry and cold... well, dry in the sky but just as wet on the track. It was absolutey carnage all day, bikes, humans, everyhwere.. delay after delay, run after run of reds... getting flow wasn't happening. More delays, more ambulances... etc. Reports in the pits of rider XYZ having done this and that, broken this, broken that.... Jeeez.
Seeding/Qualifying was massively delayed, like 2.5 hours ish. He then didn't come down at his allocated time... Oh... As a parent when the clock hits about 5 mins, your heart sinks a little.. You know how good/bad your rider is and you have a time in mind that even if they had a small slip off, they'd still come down by... He ended up coming in after 7 mins something.. But he was down and apart from looking a bit muddy, was OK.
IMG-20240414-WA0002 by
Steve Weeks, on Flickr
IMG-20240414-WA0004 by
Steve Weeks, on Flickr
He'd come off in the same spot countless others had done and waited for a gap so he didn't mess anyone up (mistake to do that really i guess) and came down. On the positives, he wasn't hurt and on Split 1 he was 19th, with Split 2 showing as 13th..
The bike was cleaned, then cleaned again, then again, lol.... new kit fitted and more and more delays, more and more ambulances.
Timing showed he'd finished 51st in Seeding which is good and bad as it means he gets to come down early in terms of riders...
But sadly that's where he finished... more and more delays meant the racing ended up being cancelled without anyone completing a run in any Cat. Results were taken from seeding times. So 51st.. bah. He'd been at the top of the hill for nearly 2 hours and eventually came down, but he was happy, he'd made a new friend up there chatting and had had a laugh
To put into perspective, his class started Sat morning with 72 riders... with 52 completing seeding..
From what i can see on the results, 110 riders were DNF or DNS for seeding... I mean WHAT !!!!! That's bonkers.
https://www.rootsandrain.com/event12569 ... a/results/
The day then went even more bonkers as the Transit wouldn't start at the lights on the boot had been left on all day... But 30 mins later we got the bugger started lol... eventually rolling home late on Sunday evening.
It was... a weekend of... character building.